I'm still on the K04+ and no issues - I was the original development car. Pretty sure I still have the loader somewhere but not sure what you are looking to do.
Anyone use a Mityvac 7201 extractor? I was only able to get about 3 quarts out, not counting anything that might be in the filter housing. I definitely got the tube inserted as far as possible but just not sure if it was actually to the bottom. I was probably a quart low to begin with. So with a...
Anyone use a Mityvac 7201 extractor? I was only able to get about 3 quarts out, not counting anything that might be in the filter housing. I definitely got the tube inserted as far as possible but just not sure if it was actually to the bottom. I was probably a quart low to begin with. So...
I've got the big Forge DV with the BSH relocation kit up to the front of the engine bay. Too busy this week to mess with it, plus I haven't driven my car in a week. I'll at least try to get some logs this week coming up.
Something strange happened with the engine sound a while back and I'm not sure if it's related or not. I finally removed the deteriorating hood liner so I mostly attributed it to the insulation being gone but under boost it sounds like a loud sucking sound. That makes sense since boost is...
Honestly I hadn't really paid attention in a long time - everything just worked really well. It still drives well and seems to pull reasonably hard but the fact that my clutch isn't slipping as easily doesn't make sense. I was the original development car for Bronson on this and we worked...
Anyone here still running DM K04+ tuning? I'm not sure if I'm having issues or not but trying to figure out how much boost I should be seeing. I haven't yet run logs to see requested boost but my slipping clutch hasn't ben slipping lately so I'm thinking I might not be running at 100%.
So I finally removed and dumped the insulation from the underside of the hood this weekend because it's been sagging for a long time. Then today I swore I had a massive boost leak as I heard this obvious whoosh whenever I boosted over 0psi. It wasn't until I got home and opened the hood to...
I had this exact problem about a month ago. It would lock with the fob but not unlock although I could reach inside and open it with the handle. Eventually the door stopped locking completely. I've got this on my to-do list...
So this just happened...
The little ball joint nipple literally pulled out of the fitting. It must have been working it's way out for a while but I never noticed it. It definitely enlarged the hole to the point where it can't be secured again. Anyone deal with this before? If I can't get...
My driver side rear door just stopped locking within the past couple weeks. There was a period where it would only unlock about 50% of the time. Ugh - wasn't ware this required the outsider door skin to be removed but doesn't look too tough. Anyone got a good suggestion for sourcing a new...
Thanks - are these the bushings and strut mounts you mention?
https://www.ecstuning.com/b-febi-parts/front-upper-strut-mount-priced-each/8j0412331~feb/
https://www.ecstuning.com/b-whiteline-parts/control-arm-lower-inner-rear-bushing/w53514~wtl/...
Old thread but new update. I just ordered a complete kit direct from Sachs for $1260 shipped - pressure plate, disc, DMF, and slave cylinder. It's been a long time coming but I recently decided to hold on to the Gti for a while longer so figured I'd take care of that slipping stock clutch...
Pure DD. I've had some mild clunks commonly when pulling out of my garage for years and just never bothered to do anything about it. I recently decided to keep the car for a while longer so looking to address a few minor issues and refresh some bits and pieces. I ended up buying the ECS kit...